Large Bellows Manufacturing

The objective of this project was to increase the volume of the cryogenic fuel bellows while simultaneously mitigating manufacturing flaws such as thinner material points and “webbing.” To achieve this goal, I first standardized the production process to address these issues as best as possible. I then devised a bellows design featuring a lower (improved) draw ratio, thereby minimizing material stretching and webbing compared to the initial mold I inherited.

The ultimate aim was to produce a higher volume bellows capable of being actuated at 25 Kelvin for 5,000 cycles without any leaks.

After

Following the standardization of the process, we achieved significantly improved results that demonstrated resilience to cryogenic temperatures. This standardization encompassed meticulous control over time, temperature, process, force, and various other parameters. With this process refined as possible, we successfully manufactured an almost flawless bellows featuring a smaller draw ratio and a larger volume. It served as a crucial steppingstone toward the development of the higher volume design, which are the images at the top of this page. Below, you can observe the testing of the smaller standardized bellows submerged in liquid nitrogen.

Unfortunately, I left Hyper before the large dewar that we needed to test the large volume bellows was delivered.

You can read about it here.